Strange Noise from my Alternator?
#16
redid the intake got a shorter filter and put my bigger MAF on it. got the bypass routed in and the flutter problem fixed with the BOV. and started tuning got the a/f and timing set then fouled out a plug and it misfired twice at about 4500rpm so we let off and went through what it was. fuel was good timing was good scanner didnt pick nothing up there wasnt a hard knock or rattle and didnt do it before on the previous pulls so he gonna pull a couple plugs tomorrow and check em. but we are 99% sure it was just one plug had fouled out. from the boost it was making @ 4500 were expecting 11Psi on stock 3.70 pulley that came with the kit
#18
#19
#20
got some vids ill compile and upload later when i get back to Dallas. i need to go to tr6 plugs the motorcrafts that came with it are getting hot. but 1st gear pull made 181hp 410tq 2nd made 272hp 312tq this is at 8psi 10-11degree timing and 4500lb loaded mustang dyno. so not sure what my peak will be in 3rd. a/f is was 11.2-11.6 at WOT
Last edited by Faster150; 01-25-2009 at 04:27 PM.
#22
im switching to NGK TR6's the motorcrafts that came with this kit. we believe is causing the issues with spark blow out and detonation on top end about every other pull id feel a bang out. so next weekend im gonna ohm test my wires and replace the plugs gap em to .025 and see if it fixes the issue. if not then i might have a coil pack that is flaking out.
Last edited by Faster150; 01-26-2009 at 12:08 AM.