The worst sparkplug you've ever seen?
The worst sparkplug you've ever seen?
Uh, so I'm a little worried. This the the first plug from the driver's side of my '01. The truck appeared to be unmodded when I bought it 2 months ago, I checked out the lower pulley bolt and the snout pulley, both appear to be untouched/unmarred. Since I've owned the truck I've put on a MAC hot air intake and MAC catback, and I ran the stock Predator perf. tune for a few days, then switched to the 10%+ fuel and 10%- timing because I thought I heard a slight ping once when I was really getting on it passing a concrete barrier on the highway.

It's not the best picture, but you get the idea. There's a big growth of white hanging off one side of the ground.
They appear to have been in there all 33,000mi of the truck's life, the electrode is all worn down on all of them and there is paint on the top of each plug. Green on the passenger side and white on the driver side. This is the only plug that looked like this, the other ones were a mixture of either all tan, or half tan, half kind-of white. Nothing like this though.
Tell me it's not something serious, maybe just a clogged fuel filter? I bought the filter and tool to take the old one off tonight, I'm going to change it out before I drive it again.

It's not the best picture, but you get the idea. There's a big growth of white hanging off one side of the ground.
They appear to have been in there all 33,000mi of the truck's life, the electrode is all worn down on all of them and there is paint on the top of each plug. Green on the passenger side and white on the driver side. This is the only plug that looked like this, the other ones were a mixture of either all tan, or half tan, half kind-of white. Nothing like this though.
Tell me it's not something serious, maybe just a clogged fuel filter? I bought the filter and tool to take the old one off tonight, I'm going to change it out before I drive it again.
Originally posted by Bootbox
Am I blowing this out of proportion?
Should I be worried about the state of my engine's health?
I put some NGK TR6IX's in
Am I blowing this out of proportion?
Should I be worried about the state of my engine's health?
I put some NGK TR6IX's in
Should you be worried, na
It's dry, and thats what counts,

but it does look like it was running lean, (prob leaner than the other cylinders)
CAN YOU POST A PIC OF ALL OF THEM SO WE CAN SEE ???
And as said STOCK PREDATOR TUNES KILL...
BTW
The usual leaner Cylinders for a L are the back two on the Drivers Side, although I have melted others
and AS for your title
"The worst sparkplug you've ever seen"
WHIMPY WHIMPY WHIMPY.......... hehehehehehe


BTW
What the hell is the "IX" in the TR-6's ???
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my truck started skippin one day so i pulled my plugs and the front plug on the driverside was melted so i replaced all my plugs with new ones and it's still skipping it will sit and idol no problem but when you press the gas pedal it skip real bad could it be a hurt piston or valve
First off, thanks to everyone that has chimed in, I appreciate it.
I don't know why I didn't mention this in my first post but it's been running on the Ford factory program for about a week already now. I'm preparing for a pulley and RWTD tune so I put it back to stock. The plugs were a part of this prep too.
I brought my camera and the plugs to work, I was just about to get a picture of them and the battery in the damn camera died. I'll put them up after work but they're not anything like this one. Half are tan and the rest are a mix of white/tan. None of them are crusty or growing things on them like this one was.
It designates their Iridium line of plugs.
Alright, so the game plan is to change the fuel filter tonight after work, run some fuel injector cleaner through a fresh tank of Chevron 93, and check up on the plugs when I'm putting the pulley on 'er in a couple of weekends from now.
Those of you that have posted pictures that make my plug look healthy in comparison, are those engines still with you? Or are all of those what you all found when you pulled the plugs after blowing up?
Originally posted by AZ fun
I would get rid of that stock predator tune. That right there will cause you problems right away.
I would get rid of that stock predator tune. That right there will cause you problems right away.
Originally posted by Rob_02Lightning
CAN YOU POST A PIC OF ALL OF THEM SO WE CAN SEE ???
CAN YOU POST A PIC OF ALL OF THEM SO WE CAN SEE ???
Originally posted by Rob_02Lightning
BTW
What the hell is the "IX" in the TR-6's ???
BTW
What the hell is the "IX" in the TR-6's ???
Alright, so the game plan is to change the fuel filter tonight after work, run some fuel injector cleaner through a fresh tank of Chevron 93, and check up on the plugs when I'm putting the pulley on 'er in a couple of weekends from now.
Those of you that have posted pictures that make my plug look healthy in comparison, are those engines still with you? Or are all of those what you all found when you pulled the plugs after blowing up?
YES, mine was fine after it. I did that back in the summer of 02,
Raced the schitt out of the rest of that season, all of 03 and 04. Motor came out in winter of 04 and it was still running stronger and faster than ever before. Same motor is now built and back in using the original heads, cams, + block.
Raced the schitt out of the rest of that season, all of 03 and 04. Motor came out in winter of 04 and it was still running stronger and faster than ever before. Same motor is now built and back in using the original heads, cams, + block.
Originally posted by speed12
my truck started skippin one day so i pulled my plugs and the front plug on the driverside was melted so i replaced all my plugs with new ones and it's still skipping it will sit and idol no problem but when you press the gas pedal it skip real bad could it be a hurt piston or valve
my truck started skippin one day so i pulled my plugs and the front plug on the driverside was melted so i replaced all my plugs with new ones and it's still skipping it will sit and idol no problem but when you press the gas pedal it skip real bad could it be a hurt piston or valve
Probabaly wouldn't be a bad idea to swap out the fuel filter too.
Originally posted by Rob_02Lightning
YES, mine was fine after it. I did that back in the summer of 02,
Raced the schitt out of the rest of that season, all of 03 and 04. Motor came out in winter of 04 and it was still running stronger and faster than ever before. Same motor is now built and back in using the original heads, cams, + block.
YES, mine was fine after it. I did that back in the summer of 02,
Raced the schitt out of the rest of that season, all of 03 and 04. Motor came out in winter of 04 and it was still running stronger and faster than ever before. Same motor is now built and back in using the original heads, cams, + block.



