Installed 6lb pulley (etc) boost problem
Installed 6lb pulley (etc) boost problem
Ok. I have installed a 6lb pulley, autolite plugs, magnaflow exhaust, K&N filter, and FT valve body. No Chip. So after the install today I took the test drive. I was told the truck would run fat and it needed a tune, but i cant get on the dyno untill tuesday am. So anyway the truck is showing like 6 lb of boost on the stock guage (several wot attempts both rolling and from a stop). A couple of times i got the truck to bury the boost guage but it's only doing it once in a while. When it does go into full boost it feels like its building more power than when it reads 6 lbs. (In other words i doubt it is the guage.) I have not done the dyno tune, or had the chip reburned for the pulley, but shouldnt the boost still be there? Why the part time boost?
Hope i have described the problem well enough.
Can anyone offer any ideas?
Hope i have described the problem well enough.
Can anyone offer any ideas?
The stock in dash gauge is junk! Mine did the same thing, sometimes it worked, other times it didn't.
I finally got one of those mechanics vacuum/pressure gauges and taped it to the windshield for a test drive, and then I knew for sure!
Now I have the AutoMeter with peak readout.
I finally got one of those mechanics vacuum/pressure gauges and taped it to the windshield for a test drive, and then I knew for sure!
Now I have the AutoMeter with peak readout.
I have been planning on getting a bigger guage, and i hear what you are saying.. problem is i can feel a big difference between the 6 lb reading (wot) and the off the guage reading (14 lb) at wot.
Call me nuts but thats my story.
It's like it is dumping the boost 80% of the time.
Call me nuts but thats my story.
It's like it is dumping the boost 80% of the time.
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I test drove the truck with another lightning owner (he had a modified 99 and now has a modified 02) Niether of us heard anything that sounded like detonation at any time. The truck is running fat.
I dont see how he is dumping boost on the stock pcm as the shift points arent being altered. He would still see that gauge peg regardless @ 14-15 psi
Last edited by Flying Mofo; Jun 21, 2003 at 12:00 AM.


